Zarrin
Members
- Jan 8, 2016
- 395
- 69
I was pretty excited to break down my MK18 mod 0 for the first time in a few years, service it and install some new bits n bobs. Did the same a couple of weeks ago to the MP5, while that went flawlessly, this did not.
This is more of an after action report than a request for specific bits of help, however feel free to chime in with any suggestions.
Out with the old, in with the new:
- Basic ACM 8mm 'SB' v2 shell out - Classic army 9mm QD shell in (possibly out of a scarab or nemesis)
- SHS 8mm bearing bushings out - SHS 9mm bearings in
- Old CA M15 gears out - ZCI advanced bearing gears in
- Old bog standard 3/4 cylinder out - possibly a nickel plated one in - hole location somewhere between the 3/4 and 1/2 (on paper better suited to a 250mm inner barrel)
- Old CA yellow poly-carbonate piston and piston head out (a bit shredded at this point) - replaced with a decent looking nylon one I had in my box of spares.
- Element single O-ring cylinder head out - un-branded aluminum double O-ring Cylinder head in.
- Tappet plate and spring also replaced - quite a bit of wear on both tbh (smushed back of tappet plate where it contacts the sector and the spring just felt a little too soft).
- My own flat hop out - ML Macaron 60 in (might swap this back - this mk18 is was a laser as is - why do I rip things out for the sake of ripping things out?!? dumbass)
First issue - the GB would not fit in the lower - quite a bit thicker overall than the old ACM shell - bit of dremel action on the lower receiver around the wear marks fixed this.
Reassembled, fired and the piston got stuck right at the back of the shot cycle and the motor whines horribly.
Open it up and notice there is excess plastic on the rear track both sides of the piston - clean that up, assess everything, cycle the system manually, check engagement - everything looks fine.
Back together in the lower with pistol grip on. test fire and everything seems pretty good - adjusted motor height got it going at a really nice crisp sweet spot.
Only odd thing at this point is that the shot cycling in semi auto is as follows: first shot finishes at probably 90% pre cock, next shot finishes correctly with piston all the way down the cylinder: these two starting positions repeat 100% of the time in order (mosfet is a very basic King arms no frills, AB or pre-cocking on this thing)
Finished reassembling, and the same again, after one or two shots, piston stuck at the rear of the track and a nasty whine - But it was okay one minute ago! - Aha! maybe the stock screw! - remove the stock tube - everything works again. So I reattach the stock but tighten the screw little by little into the back of the spring guide until I can force the same malfunction - this worked - I backed it out a little upon getting it to break and it seems to work fine - however the screw is already walking it's way out (can tell as the stock tube is already starting to wobble ?).
Either way, get it all back together - test fire on the chrono and nothing - refuses to feed now, looking down the mag well I do reckon the nozzle is not getting pulled all the way back and letting BBs in, but I dunno.. maybe the new tappet spring? pfff.
Either way that was me done for weekend, will pick it up again on Saturday - fu gun.
This is more of an after action report than a request for specific bits of help, however feel free to chime in with any suggestions.
Out with the old, in with the new:
- Basic ACM 8mm 'SB' v2 shell out - Classic army 9mm QD shell in (possibly out of a scarab or nemesis)
- SHS 8mm bearing bushings out - SHS 9mm bearings in
- Old CA M15 gears out - ZCI advanced bearing gears in
- Old bog standard 3/4 cylinder out - possibly a nickel plated one in - hole location somewhere between the 3/4 and 1/2 (on paper better suited to a 250mm inner barrel)
- Old CA yellow poly-carbonate piston and piston head out (a bit shredded at this point) - replaced with a decent looking nylon one I had in my box of spares.
- Element single O-ring cylinder head out - un-branded aluminum double O-ring Cylinder head in.
- Tappet plate and spring also replaced - quite a bit of wear on both tbh (smushed back of tappet plate where it contacts the sector and the spring just felt a little too soft).
- My own flat hop out - ML Macaron 60 in (might swap this back - this mk18 is was a laser as is - why do I rip things out for the sake of ripping things out?!? dumbass)
First issue - the GB would not fit in the lower - quite a bit thicker overall than the old ACM shell - bit of dremel action on the lower receiver around the wear marks fixed this.
Reassembled, fired and the piston got stuck right at the back of the shot cycle and the motor whines horribly.
Open it up and notice there is excess plastic on the rear track both sides of the piston - clean that up, assess everything, cycle the system manually, check engagement - everything looks fine.
Back together in the lower with pistol grip on. test fire and everything seems pretty good - adjusted motor height got it going at a really nice crisp sweet spot.
Only odd thing at this point is that the shot cycling in semi auto is as follows: first shot finishes at probably 90% pre cock, next shot finishes correctly with piston all the way down the cylinder: these two starting positions repeat 100% of the time in order (mosfet is a very basic King arms no frills, AB or pre-cocking on this thing)
Finished reassembling, and the same again, after one or two shots, piston stuck at the rear of the track and a nasty whine - But it was okay one minute ago! - Aha! maybe the stock screw! - remove the stock tube - everything works again. So I reattach the stock but tighten the screw little by little into the back of the spring guide until I can force the same malfunction - this worked - I backed it out a little upon getting it to break and it seems to work fine - however the screw is already walking it's way out (can tell as the stock tube is already starting to wobble ?).
Either way, get it all back together - test fire on the chrono and nothing - refuses to feed now, looking down the mag well I do reckon the nozzle is not getting pulled all the way back and letting BBs in, but I dunno.. maybe the new tappet spring? pfff.
Either way that was me done for weekend, will pick it up again on Saturday - fu gun.
Last edited by a moderator: